The initial assembly was at best a little frustrating but we got very good at doing it after thirty or forty times trying to discover what was happening inside. We were thinking we needed to make the casing out of clear Plexiglas to make it possible to debug this thing.
The first thing we discovered was that our cocking switch worked just fine. We made our cocking switch as a separate piece and milled the slot straight through rather than on the same radius as the cocking ring. We were not sure if the button head screw would bind. It didn’t!
Making the cocking switch this way was much easier and eliminated the need for the square bushing. This was a combination of Cutter\'s design with Brian\'s modification
We next found that in the safe position the button head screw on the hammer was hitting the leading edge of the cocking ring. To correct this we just milled a small ramp on the leading edge of the cocking ring that was .015†at the front edge tapered to .000†over a length of approximately .125â€.
The gun rotated very smooth with a single bolt in both the safe and fire positions. As we added bolts it became clear that we had way too much firing pin spring pressure. So we decided to put bolt 1 and 6 in the gun and head to the firing range. I just need to prove to Brian that it will shoot so I don\'t have to leave the country.
Since we do not have the magazine or top cover done we fed the rounds by hand. Bolt one fire once and misfired every other time. It was obvious that the firing pin was to short and not hitting far enough into the rim. Bolt six fired 12 rounds without a misfire. All of the rounds ejected without fail including the misfires. Overall we are very pleased with the initial test firing.