To finish the cams we needed to cut the slot for the bolt extractor. We used the same fixture that we used to mill the cams on the CNC mill. When it was in the CNC we milled a reference flat at 0 degrees on one side and at the 15 degree offset where the slot is cut for the bolt extractor. Using the zero reference we indicated the fixture, drilled and reamed two holes for 3/16 dowel pins. We set the fixture up in the vise with the pins on a parallel and milled the slot in the back cam. We then turned the fixture upright with both cams on it and did the front cams to match the back.
Now, for the big however, the 1144 stress proof is not totally stress proof. After we cut through the back cam and took it off of the fixture it closed up .035â€. Both side curled in and closed, although the one side did curl more than the other. This means the bolt extractor will not fit in the slot and the cam is curled inward toward the bolt carrier. This caused many hours of frustration, consternation, and anxiety.
Brain decided to turn another cam blank oversized, cut the slot, turn to final size and part it off. Unfortunately it did the same thing. Next, we took a jack and spread the cam as shown but it would just spring back when we took the jack out so we will try cutting a slot opposite of the bolt extractor slot but not completely through to see if we can spread it and get it to stay.